Windows and Kitchen Floor

There is definitely a sense of community inside Camp Washington. One of my fellow board members, Lacey, is tackling her own fixer upper project and several months ago shared she’d be removing  some pine flooring in her house.  This week she got started on that project and drop by my house to let me know I could come and get it, if I still needed it.  I cringe every time I look at my kitchen floors, so I most definitely do.  Sunday I picked it up and spent the afternoon pulling nails.

Her boards are wider than mine (same width as my upstairs floors), so I’ll need to rip them down to size as I did when I used my boards to patch holes in other areas downstairs.  My former neighbor did this work for me last time, but now that I’m elevating myself out of novice carpenter to advanced, I’ll tackle this myself.  Last year I caught a great deal on a router and router table, but had never taken it out the box.  This project will give me my first chance to use it.

I also got two of the first floor windows dressed; rear of guest bedroom and side living room.  If these two are any indication the prepping for installation is going to take much more effort than the upstairs.  The few contractors I did use on this project showed no regard for my piles in the basement.  They slung my organized piles around, stood on top of them, so my fears of damage manifested.  Both of those windows had significant pieces cracked off.  Fortunately, in both cases I found the cracked off piece laying on the ground near by.  Hope that holds true moving forward.

These pieces were more than dusty, so Murphy Oil soap wash down was just the first step.  The house had aluminum windows that must have been pretty drafty as these pieces of wood were riddled with staples and adhesive weather strips.

They also had screws that left large holes, so not only did I have to glue broken pieces back on I had to use wood putty to fill large holes.  All this extra work made what was a day project upstairs, multiple days.

Once I got them cleaned with the denatured alcohol I could see that this wood was also dryer than upstairs and even water damaged (I’m sure sweating occurred around these windows exposing wood to moisture).  Since I knew the putty I used was going be highly visible I decided to try something different.  I have about a half-quart of the custom color Zar Gel Stain used on the front door left, so I decided to rub all the pieces with steel wool dip in the stain.  After a day of letting the stain dry, I rubbed them with the Howard’s Feed and Wax.  Miraculous results.

Two down, nine to go.

Humpty Dumpty

20170729_161028Stained glass frame was nailed to the wall
Stained glass frame broke into many pieces when removed prior to wrecking ball
All of Venus’ skills and help from Wood Shop Scottie
Helped put stained glass frame back together again.

The picture to the left was taken prior to demo.  I was able to get the stain glass out for repair without removing the frame, but when it came time for drywall I had no choice but to remove it also.  I started with a crowbar and the dried wood started cracking immediately.  I then pulled out my reciprocating saw and didn’t fair much better.  End result about 15 pieces.

Why I waited months after it came down to start putting it together I don’t know, but I didn’t start gluing pieces together until just weeks before my move.  The base of the frame was originally in two pieces; a right and left half to create the oval.  The outer trim was originally in four pieces, a top and bottom to each side, so basically my goal was to get back to 6 pieces and then down to the two halves.  I glued small pieces together first and used my pin nailer to hold them in place.  In the final stages of the project I regretted my over use of nails.  I should have invested in more clamps.  

With relative ease I got all the smaller pieces back together and I felt I was ready for stain, which I did before nailing the trim to the base.  On side the trim stayed in tack with the base except for a section where the base and trim had broken off.  The other side the base basically shattered, but the two pieces of trim stayed whole.  With the shattered half back together I was ready to reattach the trim and the top was a perfect fit.  The bottom trim did not and I assumed the weeks of separation and improper storage caused it to warp.  I did days of online research about bending wood, but ultimately decided to clamp it and slowly tighten.  When the trim met the base I filled it with nails and held my breath when I removed the clamps.  Initially huge success.  I turned my sights to the other half.

It appeared I had lost a small slither of would, so I got the brillant (NOT) idea of using 2-part epoxy to fill most of the void and then used a product called Quickwood, on top in hopes it would blend with the wood.  Quickwood is a putty epoxy that looks like a tootsie roll with the flavor in the center.  You cut off the amount you need, kneed it until the two colors are thoroughly mixed, and then press it into the area of repair. Once it was hard I sanded it down until it was smooth with the original surface.  The experiment worked and I had two halves ready for hanging, but they no longer lined up.  One side was about a half inch longer.  Time to take this project to the Wood Shop and ask Scottie for help.


I had to remove the trim again, which brought into realization that I used way too many nails.  Nails are a detriment to some tools in a wood shop so I had to work to get as many out 20190406_154320as possible.  Of course I broke a perfectly good section of the outer trim in the process.  Also the initial huge success I had with clamping and forcing the trim to bend created a stress crack on the base.  This project was taking many steps backwards.

Scottie decided my best option was to make the base one piece and had me go to Home Depot for mending plates which we screwed and glued to the back of the frame.  We also took a very sharp chisel and removed my epoxy experiment.  Turns out I probably had not lost the piece.  We used the stress crack and the re-separation of my epoxy mend to make sure the two halves met and secured the plate with screws and Gorilla glue at the seam.  He advised that I should let that sit overnight, so this project was going to take another week. 

Turns out at my next wood shop class I was a solo act, so we got to focus on the frame.  With the two sides meeting properly the next tackle was making sure the trim would fit.  Scottie has a great eye and was able to see if we shaved a little bit of one piece with a jigsaw and sand another part with the belt sander that everything would meet.  I did everything he suggested and we used two more mending plates and wood glue to secure my former epoxy spot and the new stress crack I created.  Another overnight drying period, so the finish would need to wait for open shop.

Everything dried and I finally had a complete frame.  I was good to go home and stain, but Scottie saw and knew that I could make it better by using the Quickwood to fill where I had slight separation at some of the mended spots and to fill the original and new nail holes I created.  He showed me the proper way to apply it, so I wouldn’t have to spend as much time sanding.  The trick is moist fingers to help smooth and push it into the crevices you’re trying to fill.  I was fearful of breaking it again, but I took his advice and spent the bulk of open shop fine tuning.

Once back home I added the Quickwood to a few more areas and sanded it more.  After sweeping away the heavy dust, I used a Gerson TACK cloth (my neighbor Bill hooked me onto these) to remove all the fine dust.  I applied a coat of Minwax Pre-Stain Wood Conditioner (mainly because I had it and thought it couldn’t hurt) and then applied the custom Zar color stain, again.   I just stood back in awe, it was beautiful.  I decided to add a couple of coats of Minwax Polycrylic too.  I love working with that product and can’t wait to tackle my built-in.

While that dried it was time for me to deal with the drywall around the window casing.  It protruded beyond the casing, which meant I’d have a gap between the wall and the frame.  This situation is with most of the windows in the house.  Plaster could be spread to fill where it was needed, so some areas were thicker than others.  Drywall doesn’t give you that play, so I have some windows where it protrudes and others where it recesses. 

My favorite handyman, Tom Milfeld, just happened to see me in the yard, so I had him help me trace a line around the areas with the gaps and he suggested I use my Ridgid JobMax tool to remove the drywall and that is exactly what I did.  It actually created the perfect ledge for the frame to rest in, so hanging it by myself was really easy.  After getting the frame up I also put the back boards back around the built-in bench.  I can’t be more pleased with how this turned out.  Humpty Dumpty back together again.

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Dead Space to Closet Space

There is one TOTALLY complete area in my house, the master bathroom linen closet.  I’ve been psyching myself out.  The piles of trim and moulding in my basement has had me overwhelmed, so I’ve been avoiding it until this week.  If all the trim reinstall goes this smoothly I’ll be the happiest DIYer on the planet.

For those that have not been following the entire journey or if you need a refresher, the linen closet in my master bath was dead space behind walls that was revealed during demo.  Thanks to Pinterest I got the brilliant idea to replace this crawl space closet (I have two others that are even bigger) by inserting a dresser into the wall, see inspiration, in my master bedroom.  This meant I was able to relocate the door and moulding  and use it to create the linen closet in the bathroom.  I had to patch the missing floor and frame out a wall to create the space.  Check out the picture slideshow at the bottom of Have I Said Lately How Much I LOVE Restoring This House post.

The moulding and shelve brackets from that closet have been sitting in my master floor, with nails still in them waiting to puncture my foot, since December.  I thought it would be quick pull them out, use my tried and true Restor-A-Finish clean-up method, and nail them up in new closet.  Unfortunately I learned that the new closet was actually wider by 6.5″, so the shelve and moulding would be too short.  What to do?????

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I started by hanging the shelve brackets.  I didn’t concern myself about the gaps on the end of each center bracket because there was still more than enough support for the shelve.

To clean up the brackets, I just used Murphy Oil Soap and water.  The moulding I cleaned with the denatured alcohol in preparation for the Restor-A-Finish, but they didn’t look like they needed it.  Instead I wiped them down with Howard’s (same company for the Restor-A-Finish) Feed-N-Wax.  This company makes an awesome line of products.  The Feed-N-Wax worked GREAT, so much so that I used it on the door too as it was in far better condition than other doors I’ve restored.  I will most likely do this process (Oil Soap to remove dust and Feed-N-Wax) on more doors in similar condition.

The closet is wider, so I needed to extend the floor moulding center piece and for that I used a piece of the moulding that was on the opening (door) side.  I decided to not trim out the inside of the door, which freed up some extra moulding.

To extend the moulding I cut one end of the long piece to a 45 degree angle and glued the 6.5″ extension, also cut at a 45 degree angle to it.  I used a product called Insta-Bond, that my carpenter, Tom Milfeld, told me about.  I’m not 100% sold on this product; I’m batting 50/50 on it holding, but it held on this and you can barely tell where the splice meets.

Next up the shelves.  Only one of the two were still in the house and unlike the brackets I could not use the original due to the bracket design.  Instead I went to Home Depot and bought a 4′ x 8′ sheet of pine ply-wood and had them cut it in half and down to 64″ in length (only way to get it in my car).  To make the front edge look finished, I also purchased 1/4″ x 3/4″ pine moulding that I glued and pin nailed to the plywood.  I thought I wanted extra wide shelves, given I will only have two, but once I saw the first in the space I decided to rip it down to 18″.  Still 2″ wider than original.  After a dry fit they were ready for staining.  Tip (I did not do and should have): sand the pine moulding after it’s installed.  1) to get rid of any glue residue and 2) that brand seems to have a waxy film on it that does not absorb stain well, which I knew from past projects.  I was just eager to get this done and didn’t take the extra time.

I used Zar wood stain in Early American that I bought from Sherwin Williams for the kitchen built-in.  This was a great way to see if I had been recommended the right color and I believe it is, so I’m anxious to start working on the built-in again.  Britt Sang, door painter/stainer, used Minwax Polyacrylic on the inside of my front door and gave me the leftovers.  I decided to use it on the shelves, just to protect them a bit. I had never used this product, but will use it again on the built-in.  It was very easy to use and, unlike oil-based polyurethane products I’ve used, did not smell and dried fast.  I applied three coats, sanding lightly with 220 grit sandpaper between each coat.  It only needed 2 hours of drying time between coats, so this part was done in a day.

They recommend allowing 24 hours before actual use, but I placed in the closet and throw in two sachets of lavender to hopefully nix the faint chemical smell.  I did wait before placing my contents.  Thrilled with the end results and re-energized to tackle more.

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